Engineering Notebook – 02/14/2019





  • Adjust the current positions in the code to allow the new bucket to work with the current autonomous programs.
  • Troubleshoot and fix any problems that the robot might have in the code or structurally before the next qualifier.
  • Practice driving and operating the robot with the new attachments.

Meeting Notes Alex

  • To make sure that the new bucket would work we made a new program to extend the x-rail and dump the team marker with the new bucket design. Because this worked when we tested it separately we changed the Gold_Marker_Crater_Auto program to incorporate the extension of the x-rail in order to drop the marker in the depot.
  • At the end of the meeting when we were testing the new bucket we realized that it was more inefficient and harder to use than the original bucket.

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